Recent content by Wals0248

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    VMP Customer Service

    I think I had a P219A code pop up maybe 2 or 3 times but it hasn't done it in about a year. I had a couple questions concerning some other issues as well and I think they responded as quickly as they could and answered my questions thoroughly.
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    First dyno

    Thanks! Yeah, its pretty good, just make sure the steering wheel is straight before you hit it!
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    First dyno

    I'm still on the stock manifolds and cats. VMP said they could put me on a 93 tune and 79mm pulley, just need a boost a pump. I'm debating that or headers. I have a borla atak axle back so I'd have to figure something out for noise, its already pretty bad/amazing at WOT.
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    First dyno

    Nothing super crazy but this is the first time I've ever had my car on a dyno, I installed the VMP kit last year, its a 13 GT M6 with a gen 2 r and a 85mm pulley on a 91 octane tune. The sae number was 566 peak rwhp. For comparison we had a stock 2012 GT M6 dyno right after this one that put...
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    Thoughts on a Clutch

    Exedy Mustang Mach 500 Stage 3 Clutch 07807LB (11-14 GT) I think this is what I went with. 2013 GT with a Gen 2R, drives like stock and holds power just fine. Depends on how crazy you're going to get though. I put a new Ford slave cylinder in but left the flywheel alone, it only had 40k on it...
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    High RPM lockout...more pronounced after supercharger install...clutch change?

    Exedy Mustang Mach 500 Stage 3 Clutch 07807LB (11-14 GT) I have a 2013 GT with a VMP on it, I went with this one, drives like stock. I should also add I replaced this before I did the supercharger because the pedal was sticking to the floor. I think my 2nd gear syncros have had their life cut...
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    Intermittent issues after VMP Stage 1 install - limp mode and P219A code

    I did the same install on my 13 GT, I'll periodically get this code, mostly gone away at this point. Maybe make sure the intake is snug?
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    Lost performance

    I don't think it's anything to be worried about, just the system naturally burping itself and settling, I should have kept a closer eye on it
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    Lost performance

    Just gotta keep it simple!
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    Lost performance

    Well, didn't want to wait. I think it's fixed, most likely the low coolant. First time I got on it in second the tires just eviscerated. Much cooler iats. All around more power!
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    Lost performance

    New theory, could just be a combination of a few things, air filter was slightly loose, maf has been cleaned, the foam insert for the jlt intake had become unlodged in the cai, lastly but most importantly, I also noticed the coolant in the heat exchanger reservoir had dropped(I don't think I...
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    Lost performance

    So I pulled the passenger side plugs and they're pretty black. Maybe try a new set? Here's a picture 20190925-161650
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    Lost performance

    It's a hydraulic clutch, fresh fluid, slave, and braided line. I feel like a slipping clutch would be more evident, I think its an exedy stage 3 if I remember correctly.
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    Lost performance

    I checked the lines last night and gave the maf a good spray clean. I think the air filter clamp was a little loose. It definitely hit 8.5 psi on the gauge this morning. Still seems a little soft, I might try to get a dyno run in. I have a friend with a 12 that would be interested and it would...
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    Lost performance

    I've got a gauge, and while its hard to watch it really close when driving, the needle appears to indicate the correct amount of boost 7-8ish psi with an 85mm pulley. I'll check the lines over, clean the maf and worst case maybe plug the gauge to see if it makes a difference

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