Here is the story,
I have a new JLP longblock and a Whipple running 75# injectors and fuel rails, TR6's gapped at 30, stock coils, E-fan, dual 255's, JDM fuel system upgrade, ect...
I went for a dyno tune and the tune went good with the first combination 8# lower and 3.375 upper. About 575rwhp and 595tq with 15deg and 11.8 or so AF with a max of 5200rpm's. We saw about 17.5#'s of boost. We added in race fuel and changed to a 2.7 upper with the 8# lower and the truck shuts off at 3000rpm's like you turned the key off mid pull. At first I thought something happend to the motor because when we went to refire it backfired and I didn't want to take a chance on hurting the new motor. So I removed the Whipple checked plugs checked compression (130-140) and borescoped the cylinders. All was good so I put it all back together. We went to the dyno and same thing happend with the 2.7 upper the second time so we put the 3.375 upper back and all is fine.
Durring both pulls when the truck shuts off it is around 3000rpm and fuel pressure, maf counts, and AF all look perfect just like the 3.375 pulley tune. When it shuts off it's only at about 335rwhp and 500+tq. It dies just like someone shut the key off that is the confusing part since it's only with the small pulley.
The second time it shut off it threw a p1114 code AIT2 voltage to low but when we cleared it and went to the 3.375 upper it did not return and the pull made the same power as it did the first time we had the 3.375 pulley on.
Please shoot me some ideas I'm stumped.
Dan
I have a new JLP longblock and a Whipple running 75# injectors and fuel rails, TR6's gapped at 30, stock coils, E-fan, dual 255's, JDM fuel system upgrade, ect...
I went for a dyno tune and the tune went good with the first combination 8# lower and 3.375 upper. About 575rwhp and 595tq with 15deg and 11.8 or so AF with a max of 5200rpm's. We saw about 17.5#'s of boost. We added in race fuel and changed to a 2.7 upper with the 8# lower and the truck shuts off at 3000rpm's like you turned the key off mid pull. At first I thought something happend to the motor because when we went to refire it backfired and I didn't want to take a chance on hurting the new motor. So I removed the Whipple checked plugs checked compression (130-140) and borescoped the cylinders. All was good so I put it all back together. We went to the dyno and same thing happend with the 2.7 upper the second time so we put the 3.375 upper back and all is fine.
Durring both pulls when the truck shuts off it is around 3000rpm and fuel pressure, maf counts, and AF all look perfect just like the 3.375 pulley tune. When it shuts off it's only at about 335rwhp and 500+tq. It dies just like someone shut the key off that is the confusing part since it's only with the small pulley.
The second time it shut off it threw a p1114 code AIT2 voltage to low but when we cleared it and went to the 3.375 upper it did not return and the pull made the same power as it did the first time we had the 3.375 pulley on.
Please shoot me some ideas I'm stumped.
Dan