Started doing a retest with the engine warmed up. First hole and I pulled the hose right off the end of the adapter that screws in the plug hole. SMH. There's no way this thing is accurate or consistent. We are talking 150+ psi. And I just pulled it apart.
Also there is oil pooling in my intake tube at the throttle body. Is this normal on these engines?
Anyway, what are the odds a ruined this engine. I have made 2 wot pulls half of second and half of third gear. And one wot pull 1-2 gear. All before I was told it runs lean after 4K. I know there is no way to no for sure but what's the likelihood I hurt something with such minimal exposure to lean conditions. I am just scared here.
Also there is oil pooling in my intake tube at the throttle body. Is this normal on these engines?
Anyway, what are the odds a ruined this engine. I have made 2 wot pulls half of second and half of third gear. And one wot pull 1-2 gear. All before I was told it runs lean after 4K. I know there is no way to no for sure but what's the likelihood I hurt something with such minimal exposure to lean conditions. I am just scared here.